The Exergy and Energy Analysis of Change Phase Steam in Patuha Geothermal Well Production

Mochammad Fa'iq Khasmadin, M. S. K. Tony Suryoutomo, Gatot Yulianto

Abstract


A Geothermal Power Plant Company in West Java Indonesia have capacity around 55MW. It company have increased the well production quality to keep up the Indonesia's energy demands. The power plant has been operated around ten years, it has ten geothermal production wells and two injection wells. The either of it wells has an abnormality. It wells has water dominated condition so, the separator equipment is required to separate the steam from water and vapor. Previous study indicated that subsurface water entering the broken reservoir pipe. That leaks in reservoir pipe was repaired in 2020. The impact after the pipe have been repaired it made the fluid characteristic of reservoir be vapor dominated. After that a separator as a steam separator is no longer required. The study compares the value energy and exergy power of the power plant. The calculations are performed from the well reservoir and all power plant equipment. According to the results of the energy study, the plant's energy efficiency after the transformation increased by 0.03%, from 19.48% to 19.52%. The exergy value of the brine in either wells (separated steam cycle) is also known to be 2.512,52 kW, beyond which the value will become zero.

Keywords


geothermal; anomaly reservoir; exergy efficiency; energy efficiency

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DOI: http://dx.doi.org/10.52155/ijpsat.v42.1.5871

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